alwaysFlOoReD
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V8 Engine Swap
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- Joined
- Apr 13, 2009
- Messages
- 14,398
- Reaction score
- 5,742
- Location
- Airdrie, Alberta, Canada
- Vehicle Year
- ’97, '06
- Make / Model
- Pontiac, Dodge
- Engine Type
- V8
- Engine Size
- 2.2,5.7
- Transmission
- Automatic
- 2WD / 4WD
- 4WD
I needed a vehicle cheap on gas and that I could take to auto-cross and similar events. That means not a truck. Piss me off that all these clubs are so prejudiced against trucks. Oh well, enough bitching! I bought a 98 Neon for $60.00 with a bad knock. The body is good as is the interior, it just needs a good cleaning. In my research for racing the neon I found that there is Neon spec class ice racing. It's meant to keep costs down by specifying what mods you're allowed, in this case none. It also specs the engine which is supposed to be a SOHC. The 98 came with a DOHC so I found another Neon, a 96, for $400.00 with what I thought was a fairly good SOHC motor.
The 96 versus my current DD, a 2004 f-150 w/ 5.4l/ auto getting ~ 20.5 l/100km [ 11.5 mpg U.S.]
Some more pics
The 98-
The 96 has had a lot of work done to it in the past, there are leds all over the place and wiring for a high end stereo and other stuff dead-ending everywhere. I spent a few hours ripping out the dash and then the extra wiring that makes it hard for me to see what's stock.
When I first got the 96, it would run at a very high rpm ~3500 when cold, slowly dropping to ~1800 when warm. The rpm would jump if a load was put on the electrical such as a heater fan. I checked neons.org for possible fixes. First I checked the vacuum lines and found one disconnected at the charcoal canister. I then ran the car again and pulled codes. I got the following;
p0123 throttle position sensor switch A high
p0134 o2 bank1 sensor 1
p01351 ignition coil A primary secondary
p1391 interim loss CMP or CKP
Not really knowing what those mean I decided to look at the o2 sensors. After figuring out how to remove the intake, I saw one o2 sensor wire unhooked. I looked under the car and the second o2 sensor bung has been removed. So I decided to move the existing o2 over to the other o2 sensor wire thinking that the pcm needs the first o2 reading more than the second.....don't know if this is true or not- just guessing. At this time I haven't fired up the car to find out any changes.
The same afternoon I decided to check the spark plugs and found two wires soaked in oil. Pulled the plugs and found one oil fouled and another close behind. The owner had said that he had recently replaced the valve cover gasket and had screwed up on one plug-tube gasket in the process. It looks like he forgot to do one as one showed no signs of replacement. I then tried to do a compression test and was able to thread the tester into 3 of 4 holes. The test was done cold @ ~-10C.
1] 130 psi
2] n/a
3] 170 psi
4] 195 psi
It seems the upper portion of cylinder 2 has no threads left. A spark plug threads in fine but also has .5" more threading than my compression tester. I tried to adapt a gauge to my leakdown tester but didn't think of the need for a check valve so that didn't work. I'll be going back today to install some air lines so I can do a leakdown test. Then I'll button the motor back up and see what results.
Thanks for looking,
Richard
The 96 versus my current DD, a 2004 f-150 w/ 5.4l/ auto getting ~ 20.5 l/100km [ 11.5 mpg U.S.]
Some more pics
The 98-
The 96 has had a lot of work done to it in the past, there are leds all over the place and wiring for a high end stereo and other stuff dead-ending everywhere. I spent a few hours ripping out the dash and then the extra wiring that makes it hard for me to see what's stock.
When I first got the 96, it would run at a very high rpm ~3500 when cold, slowly dropping to ~1800 when warm. The rpm would jump if a load was put on the electrical such as a heater fan. I checked neons.org for possible fixes. First I checked the vacuum lines and found one disconnected at the charcoal canister. I then ran the car again and pulled codes. I got the following;
p0123 throttle position sensor switch A high
p0134 o2 bank1 sensor 1
p01351 ignition coil A primary secondary
p1391 interim loss CMP or CKP
Not really knowing what those mean I decided to look at the o2 sensors. After figuring out how to remove the intake, I saw one o2 sensor wire unhooked. I looked under the car and the second o2 sensor bung has been removed. So I decided to move the existing o2 over to the other o2 sensor wire thinking that the pcm needs the first o2 reading more than the second.....don't know if this is true or not- just guessing. At this time I haven't fired up the car to find out any changes.
The same afternoon I decided to check the spark plugs and found two wires soaked in oil. Pulled the plugs and found one oil fouled and another close behind. The owner had said that he had recently replaced the valve cover gasket and had screwed up on one plug-tube gasket in the process. It looks like he forgot to do one as one showed no signs of replacement. I then tried to do a compression test and was able to thread the tester into 3 of 4 holes. The test was done cold @ ~-10C.
1] 130 psi
2] n/a
3] 170 psi
4] 195 psi
It seems the upper portion of cylinder 2 has no threads left. A spark plug threads in fine but also has .5" more threading than my compression tester. I tried to adapt a gauge to my leakdown tester but didn't think of the need for a check valve so that didn't work. I'll be going back today to install some air lines so I can do a leakdown test. Then I'll button the motor back up and see what results.
Thanks for looking,
Richard