More Data
First RobbieD tnx for the great advice!!
I will try the trim cap removal and check the screws..
Here is what I found last night. I was not going to do much but you got me inspired, and maybe I just got to the point of frustration to try something..
Anyway...
These are the steps I did and the /// results
While the truck was running and radio on 610 or 810 the ones I listen to most here in KS:
1 put alligator clips on antenna and touched the other side to metal hood /// no change.
2 put longer clips on and tried to touch a ground spot in the engine compartment /// no change
3 Tested the "RobbieD is it loose" problem, so I grabbed the ant abt mid way up and gentle wiggled it.. /// it was solid and tight
BUT!!!!
BUT!!!!
When I did that my hand caused some "something" ( and being a ham and having a ham father I should know this.. arg) maybe the word is capacitance. Well whatever it is the signal got better... Hmm..
Ok well I read this on my searchings yesterday:
from this site
http://www.bellscb.com/products/accessories/DC_Noise_filter.htm
If you have radio noise caused by your engine (noise that increases or decreases with engine speed) this filter might help you.
Engine noise can enter your radio TWO ways. Through the power wire source and through the antenna. This filter will reduce the noise coming in the power wire.
To be sure this filter can help you, unplug the antenna from your radio and start the vehicle and rev the motor. Turn up the volume on radio and try to see if the noise went away, or at least most of it did. If the noise stays with no antenna connected this filter WILL help you allot. If the nose goes away after removing the antenna, than this filter will NOT help you. In this case you will need to filter the noise source (like the alternator or fuel pump).
Well kr@p I hope it not the antenna....
I gently open full the glove compartment and find the antenna run.
I reach as close as i can to the antenna under the dash and wiggle. /// no change
I found some colored "wires" and think abt pulling them why I dont know....Well they didnt quite go to the correct spot on the stack...
OPPS they are the AC/HEATER tubes... DOH! Whew gud thing I was slow abt jumping in...
Did not find the radio connector as I know I would not due to the dash construction....
Ok well since I am out here dorking around I might as well pull the radio stack.
Looking around the stack wondering how I am ever going to pull this without tearing it all apart and making it look awful when I put I back together I found 2 screws under the lip of the CD player I think
Took the 2 screws out. Ok so far so gud.
Well here goes. I gently wedge my fingers around the black face plate on the left.. Tight but moving.. ok go to the bottom. Better but it is very narrow and would break if I hank on it.. ok go to bottom right.. And lo and behold the face plate/stack popped a tad out... 0k ok ... so I gently work my way around the top and then back down the left...
Yippie its out.. !!!!! Cool Took the right side Cig lighter cable off, and it slid farther out......
Ok I see the ant connection.. I start to gently work it back out..
I pull the ant and the radio is very much quieter... Bummer.... (See above description) Oh well lets experiment due to what you said....
The ant connection could have been "cleaner".. By that I mean there was some flaking or some sort of foam that was old and coming off... Hmm
Here is where I dont have all my notes....
I think I reseated the ant. In doing that the signal obviously came back into the radio. But in doing that I had to gently twist the connector to seat it.
WAIT twisting the connector..... The signal improved.. ?!?!?!?!?
Wow ok so I took the connector out and tapped it against the dash and some flaking came out. That might be either here nor there but I did it just the same...
I put the ant connector back and twisted for best sig and it was fine.
I then pushed the stack back in and the ant/connector is a right angle and when I pushed the stack back the angle got more accute and pushed the ant in toward the back of the radio... There just is too much stuff in the back of the dash... Anyway I moved the ant/connector orientation and gently pushed it back to about 1/2 inch before the stack would be seated and the signal stayed the same.
I went to work this morning with it not fully seated and listened to 610 and 810 and was happy. Granted I only live 4 blocks from work but I still got listen to it.
So my next steps I think is/are to:
1 find the best orientation for the ant/connector
2 Put a block between the radio and the connector so it does not get bent toward the radio
3 fix the connector
Anyway the inline noise filter is probably not going to work.. I dont know if that is good or bad... The connector really needs fixing I think because if I put it all back and it works now I might become a problem with the vibrations of driving....
RobbieD what are your thoughts that might add to my detective work???
Will keep you posted.
Jacq..